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| Well: Ludie No. 1 | Permit No.: 47-097-03188 |
| Contractor: SW Jack Rig 15 | Spud Date: February 3, 2005 |
| District/County: Warren/Upshur | State: West Virginia |
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| Report Date: | 02/23/05 | Report Time: | 5:00 PM |
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| From: | To: | Description of Operations |
| 2:30 PM | Checked casing pressure. Found 1,540 psig. | |
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| From: | To: | Description of Operations |
| 1:30 PM | Checked casing pressure. Found 1,360 psig. Analysis of gas sample showed N2 at 5.34%. | |
| Projected Operations : Commence pipeline construction. |
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| From: | To: | Description of Operations |
| 12:00 AM | 1:30 PM | Flowed well back through 2" choke. Found well blowing hard at 1:30 PM. Collected gas sample for notrogen/gas quality analysis. Shut well in. |
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| From: | To: | Description of Operations |
| 12:00 AM | 2:30 PM | Flowed well back through 1" choke. Checked open flow at 2:30 PM, found 8/10ths H2O through 4", or about 500 mcf/day. |
| 2:30 PM | 12:00 AM | Changed choke to 2" choke. Flowed well back through 2" choke. |
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| From: | To: | Description of Operations |
| 6:30 AM | 8:05 AM | Universal rigged up frac and nitrogen equipment. Had problem with communcations to blender. Tested lines |
| 8:05 AM | 9:20 AM | Fractured Benson with 40,000 lbs of 20/40 sand using 60 quality foam. Formation broke at 2,500 psig, and treated at an average rate of 17.66 bbls/minute and an average pressure of 3,171 psig. Displaced 500 gallons of 15% HCl acid. Dropped 3.75" ball and flushed casing to perfs. Instant shut-in pressure was 2,410 psig. Five minute shut-in pressure was 2,270. (Used 468,000 scf of nitrogen on first stage.) |
| 9:20 AM | 10:10 AM | Perforated Riley (under pressure) with 19 holes from 4,101' to 4,119' with two gun runs. |
| 10:10 PM | 11:10 AM | Tried to break Riley. Took pressure to 4,000 psi. Would not break. Let soak for five minutes. Took pressure to 4,000 psi. Would not break. Let soak. Formation broke at 3,650 psi. Fractured Riley with 40,000 lbs of 20/40 sand using 60 quality foam. Formation treated at an average rate of 17.66 bbls/minute and an average pressure of 3,266 psig. Flushed casing to perfs with 26 bbls of foam and a ten bbl cap of fresh water. Instant shut-in pressure was 2,218 psig. Five minute shut-in pressure was 2,170 psig. (Used 459,000 scf of nitrogen on second stage.) |
| 11:10 AM | 11:45 AM | Rig Universal down. Install ball-catcher and 1/4" choke. |
| 11:45 PM | 2:00 PM | Flowed well back through 1/4"choke. |
| 2:00 PM | 4:15 PM | Shut well in. Broke ball-catcher and checked for frac ball. Not found. Installed 1/2" choke. Flowed well back through 1/2" choke. |
| 4:15 PM | 4:30 PM | Shut well in. Broke ball-catcher and removed frac ball. Installed 1" choke. Flowed well back through 1" choke. |
| 4:30 AM | 12:00 AM | Flowed well back through 1" choke. |
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| From: | To: | Description of Operations |
| 2:00 PM | 4:15 PM | Ran correlation log and cement bond. Found good bond, and cement top at 3,500', as expected. Perforated Benson with 16 holes over 4' from 4,558-4,562'. |
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| From: | To: | Description of Operations |
| 9:00 AM | 4:00 PM | Energy Contractors delivered on 200 bbl tank to location. Hauled water to fill both tanks. Found 900 psig on 4 1/2" casing. 100 psig on 8 5/8" casing. Pressure on 4 1/2" casing appeared to be acid gas. Blew down very quickly. |
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| From: | To: | Description of Operations |
| 7:00 AM | 4:00 PM | Rigged down. moved off location. S. W. Jack left one 500 bbl. tank to use for frac job. Noticed leak around the 8 5/8" casing. Blew it down and tightened it up. |
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| Depth | Reading | Volume |
| 2,129' (soaping) | Odor | 0 mcf/day (below Gantz) |
| 2,656' (soaping) | 20/10th H2O - 1" | 47 mcf/day (below 5th Sand) |
| 3,335' (soaping) | 10/10ths H2O - 1" | 33 mcf/day |
| 3,829' (soaping) * | 20/10ths H2O - 1 5/8" | ?? mcf/day (poor gas check!) |
| 4,536' (soaping) | 10/10ths H20 - 2" | 133 mcf/day (below Benson) |
| 5,097' (soaping) | 10/10ths H20 - 2" | 133 mcf/day |
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| From: | To: | Description of Operations |
| 12:00 AM | 3:40 AM | Drilled 7 7/8" hole, soaping. Reached TD of 5,340'. |
| 3:40 AM | 4:30 AM | Clean hole, prepare to trip out and lay down drill pipe. |
| 4:30 AM | 10:45 AM | Trip out of hole and lay down drill pipe. |
| 10:45 AM | 3:45 PM | Rigged up logging truck (Allegheny Wireline). Logged well. |
| 3:45 PM | 4:50 PM | Prepared to run pipe. |
| 4:50 PM | 7:10 PM | Ran 4,630' (109 joints) of 4 1/2" casing (10.5 lb./ft) from McJunkin, with latch down in shoe on bottom, cenralizers on joints 2,8,11,13 and 17, and a 3 9/16" baffle in the top of Joint 11, just below Riley. |
| 7:10 PM | 9:20 PM | Cemented csasing (Universal) with 210 sx of 50/50 Pozmix with 2% gel, 10% salt and 1/4# flake. Pumped plug down with 500 gallons of 15% HCl acid. |
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| From: | To: | Description of Operations |
| 12:00 AM | 12:00 AM | Drilled 7 7/8" hole, soaping. Rig was 4,335' at 7:00 AM, drilling 30 minutes per kelly. Benson in samples. Gas check at 4,536' showed 10/10ths water through 2" (133 mcf/day). Flow flucturated above 10/10ths due to fluid in hole. * (Relief) toolpusher reviewed gas check from 3,829', and indicated test was taken through 1 5/8" (non-standard) orifice. While clearly there was an increased volume of gas present, this check is not deemed reliable. Rig was 4,356' at 11:15 AM. Rig was 5,097' at 10:15 PM, drilling 25 minutes per kelly. |
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| From: | To: | Description of Operations |
| 12:00 AM | 12:00 AM | Drilled 7 7/8" hole, soaping. Gas check at 3,335' showed 10/10ths through 1" (33 mcf/day).Rig was 3,365' at 7:30 AM, making a connection. Rig was 3,576' at 1:15 PM, drilling 36 minutes per kelly. Gas check at 3,829' showed 10/10ths H20 through 2" (189 mcf/day). * Not sure I believe this gas check. Clearly, there was some gas there, but I question if the well was allowed to blow down before the gas check was taken. Rig was 3,980 at 11:30 PM. |
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| From: | To: | Description of Operations |
| 12:00 AM | 12:00 AM | Drilled 7 7/8" hole, soaping. Rig was 2,515' drilling 36 minutes per kelly at 7:10 AM. Gas check at 2,656' showed 20/10ths through 1" (47 mcf/day). Rig was 2,899', drilling 35 minutes per kelly at 6:15 PM. Rig was 3,062' at 11:00 PM drilling 40 minutes per kelly. |
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| From: | To: | Description of Operations |
| 12:00 AM | 12:00 AM | Drilled cement. Drilled 7 7/8" hole. Rig was 1,585', dusting, drilling 24 minutes per kelly at 6:45 AM. Rig was 1,829' at 1:30 PM, dusting, drilling 45 minutes per kelly in the bottom of the Big Lime. Top of Big Lime found at 1,731'. Picked up 1 1/2" stream of water at 2.004' at 5:50 PM. Started soaping hole. Rig was 2,188', soaping, drilling 30 minutes per kelly, at 11:00 PM. |
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| From: | To: | Description of Operations |
| 12:00 AM | 5:30 AM | Drilled 10 5/8" hole. Reached TD of 1,370' at 5:30 AM. |
| 5:30 AM | 7:50 AM | Clean hole. Trip out of hole. Rig up loggers. |
| 7:50 AM | 9:00 AM | Logged coal. |
| 9:00 AM | 10:45 AM | Stripped cellar. Ran 30 joints (1,325') of 8 5/8" casing (McJunkin) with two joints of 23# on bottom and one joint of 23# on top, and other 27 joints 20#. Rigged up Universal to cement. |
| 10:45 AM | 12:15 PM | Cemented 8 5/8" casing to surface with 300 sx of Class A cement. Well circulated. |
| 12:15 PM | 8:00 PM | Wait on cement. Nippled up on 8 5/8". |
| 8:00 PM | 11:40 PM | Nippled up on 8 5/8". Tripped in hole with 7 7/8" bit. |
| 11:40 PM | 12:00 AM | Drilling plug and cement. |
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| From: | To: | Description of Operations |
| 12:00 AM | 2:00 PM | Drilled 10 5/8" hole. Rig was 978' and soaping at 7:00 AM, drilling 28 minutes per kelly. Rig was 1,138' at 1:40 PM. Bit cratered about 2:00 PM. |
| 2:00 PM | 4:00 PM | Tripped out old bit, ran in new bit. Could not get to bottom. Stopped four stands off bottom. Started reaming. |
| 4:00 PM | 10:00 PM | Reaming hole. |
| 10:00 PM | 12:00 AM | Drilling 8 5/8" hole. Rig was 1,150' at 10:30 PM, drilling 60 minutes per kelly. |
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| From: | To: | Description of Operations |
| 12:00 AM | 12:40 PM | Drilled 11" hole. Rig was 249' and soaping at 7:00 AM, carrying 1/2" stream of water. Drilled to 420'. |
| 12:40 PM | 1:45 PM | Trip out of hole with 11" hammer bit. Trip in hole with 10 5/8" tri-cone bit. |
| 1:45 PM | 12:00 AM | Drilled 10 5/8" hole. Rig was 547' at 4:30 PM, soaping, drilling 30 minute kellys. Rig was 781' at 11:30, drilling 20 minutes per kelly, soaping. |
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| From: | To: | Description of Operations |
| 7:30 AM | 12:00 AM | Drilled rat hole. Drove 32' of 16" conductor. Cleaned out conductor. Rig had a compressor down. Started 15" hole with hammer bit about 4:45 PM. Set 69' of 11 3/4" casing. Nippled up on 11 3/4" casing. Rig was 81' at end of day. |
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| From: | To: | Description of Operations |
| 7:30 AM | 7:30 PM | Moved S. W. Jack Jack Rig 15 (Joe McVicker, Toolpusher) to location from Core B. Rigged up, prepared to spud. |
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| From: | To: | Description of Operations |
| 7:30 PM | 5:00 PM | Moved S. W. Jack dozer to location. Graded location. Built pit. Location complete. Waiting on rig. |
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| From: | To: | Description of Operations |
| 8:30 PM | 2:30 PM | Graded location. |
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| 7:30 PM | 4:30 PM | Grade location. Lost time due to Fighting large rocks on strip bench. |
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| From: | To: | Description of Operations |
| 7:30 PM | 4:30 PM | Grade location. Fighting large rocks on strip bench. |
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| From: | To: | Description of Operations |
| 2:00 PM | 3:00 PM | Move Exil Light's dozer to location. |